Post by spunkymonkey on May 22, 2011 19:19:06 GMT
Ok, seeing as someone asked for photos, I decided to do a thread for Harry the Hoist:
He was bought second hand by the owner of our workshop a few years back and installed as he'd been in his previous home - badly! He also had his 3-phase motor removed and changed for a single phase, which meant he couldn't actually lift anything much heavier than a Reliant Kitten. Well, not strictly true - once moving he'd lift full (2 tonne) load but he wouldn't actually start with any real load applied.
The columns are connected by a chain drive through the base, which is working ok but a little noisy thanks to a missing tensioner spring in one tensioner (the horribly emulsified oil might not help much either!):
That's a fairlyt minor point though, so can wait indefinitely while the rest is sorted!
First job in getting him working again was to learn how 3 phase motor wiring, with reverse and safety interlocks works. Won't bore you with the details but the end result was this:
3 phase motor refitted, with twin (for reversing) contactors and overload cut-out, operating by his original push-buttons. Incidentally, it seems that to reverse a 3 phase motor all you have to do is swap any two of the 3 wires. How cool is that? ;D
The problem at this point was that the top and bottom limit switches weren't working because there's (meant to be) a safety cable that runs from the carriage on the "motor" leg, over a spring-loaded pulley at the top of that leg, down and through the base, then up the slave leg to the other carriage. The cut-out switches are operated by the pulley moving up or down on it's spring mounts. The cable had broken at some point and someone had re-wired to simple limit switches at the top and bottom of the motor column.
That's all well & good but the cable has other uses. Say, for example, you're lowering a car and you've forgotten to move the trestle that's under one lifting arm. As soon as that arm hits the trestle it stops moving down - the arms just rest on the lift nuts, so they have to go up together but when lowering one can be left behind.
That pulls on the cable, which pulls the pulley down and immediately operates the lower limit switch no matter how far off the ground the arms are. So you don't tip the car off sideways by lowering it onto an obstruction.
Also, the lifting nuts have a safety nut fitted underneath them that will "catch" the load if a main nut fails, only allowing it to fall about 10mm. But that 10mm is enough to alter the cable tension and, again, operate the cut-outs so that the hoist can't be (unknowingly) operated with a defective main nut.
Being a little allergic to dropping cars on my head, I decided that he needed a new cable. Convinced his owner to fork out £14 for 30m of 3mm steel rope (a small price to pay for peac of mind!) and started to thread it. Only, it wouldn't feed through the base from the motor side, which meant lowering the leg enough to feed directly into the guide tube. Tipping around 1/4 ton on steel post over at an angle makes me a little nervous, so plenty of straps and an engine crane were employed:
That allowed enough tilt to get my fingers in under the column and start feeding cable through:
Once bolted back together, with new arms fabricated for the limit switches (photos another day), the top switch worked beautifully but the bottom one failed to operate. It was only a matter of adjustment but the failure to stop promptly broke the new cable!
Luckily, it broke very near the end and I haven't trimmed it to length yet, but I couldn't be bothered to re-do it today so called it quits for now. Hopefully, more photos and reports of a working hoist in the next couple of days - then follow-ups will show just what he can do and how easy some things become with Harry on your team ;D
He was bought second hand by the owner of our workshop a few years back and installed as he'd been in his previous home - badly! He also had his 3-phase motor removed and changed for a single phase, which meant he couldn't actually lift anything much heavier than a Reliant Kitten. Well, not strictly true - once moving he'd lift full (2 tonne) load but he wouldn't actually start with any real load applied.
The columns are connected by a chain drive through the base, which is working ok but a little noisy thanks to a missing tensioner spring in one tensioner (the horribly emulsified oil might not help much either!):
That's a fairlyt minor point though, so can wait indefinitely while the rest is sorted!
First job in getting him working again was to learn how 3 phase motor wiring, with reverse and safety interlocks works. Won't bore you with the details but the end result was this:
3 phase motor refitted, with twin (for reversing) contactors and overload cut-out, operating by his original push-buttons. Incidentally, it seems that to reverse a 3 phase motor all you have to do is swap any two of the 3 wires. How cool is that? ;D
The problem at this point was that the top and bottom limit switches weren't working because there's (meant to be) a safety cable that runs from the carriage on the "motor" leg, over a spring-loaded pulley at the top of that leg, down and through the base, then up the slave leg to the other carriage. The cut-out switches are operated by the pulley moving up or down on it's spring mounts. The cable had broken at some point and someone had re-wired to simple limit switches at the top and bottom of the motor column.
That's all well & good but the cable has other uses. Say, for example, you're lowering a car and you've forgotten to move the trestle that's under one lifting arm. As soon as that arm hits the trestle it stops moving down - the arms just rest on the lift nuts, so they have to go up together but when lowering one can be left behind.
That pulls on the cable, which pulls the pulley down and immediately operates the lower limit switch no matter how far off the ground the arms are. So you don't tip the car off sideways by lowering it onto an obstruction.
Also, the lifting nuts have a safety nut fitted underneath them that will "catch" the load if a main nut fails, only allowing it to fall about 10mm. But that 10mm is enough to alter the cable tension and, again, operate the cut-outs so that the hoist can't be (unknowingly) operated with a defective main nut.
Being a little allergic to dropping cars on my head, I decided that he needed a new cable. Convinced his owner to fork out £14 for 30m of 3mm steel rope (a small price to pay for peac of mind!) and started to thread it. Only, it wouldn't feed through the base from the motor side, which meant lowering the leg enough to feed directly into the guide tube. Tipping around 1/4 ton on steel post over at an angle makes me a little nervous, so plenty of straps and an engine crane were employed:
That allowed enough tilt to get my fingers in under the column and start feeding cable through:
Once bolted back together, with new arms fabricated for the limit switches (photos another day), the top switch worked beautifully but the bottom one failed to operate. It was only a matter of adjustment but the failure to stop promptly broke the new cable!
Luckily, it broke very near the end and I haven't trimmed it to length yet, but I couldn't be bothered to re-do it today so called it quits for now. Hopefully, more photos and reports of a working hoist in the next couple of days - then follow-ups will show just what he can do and how easy some things become with Harry on your team ;D